This morning, a new Jet 17″ in my shop started to rebel by dropping its chuck, arbor and all, while drilling 1″ deep holes with a 1/4″ forsner bit! After inspecting the arbor for residue, grit, burrs or anything else that might cause a friction fit failure (and finding nothing), I remounted the unit giving it a firm press on a scrap block of wood.
Let me back up by saying that when any new tool comes into my shop, the first thing I do is dismantle it, and check/fix any burrs, paint overspray, or any other anomaly that might keep the machine from running at its best. This was done with the new Jet Drill Press.
With everything back together, the drilling resumed. After 4 holes the chuck and arbor dropped again!
To make a long story short, I cleaned the arbor and spindle to within an inch of their lives. Blade & Bit cleaner, a stiff bristle brush, and even a very light pass with a white Scotch Bright pad. I even used a baby bottle brush inside the spindle (works great, just don’t give it back to the baby!). After a few more holes – boom! It drops again. Time to call Jet.
The tech service rep has a new arbor on its way, no questions asked.
Here (after a long winded introduction) is the new drill press trick I learned today. The tech suggested that to get the drill press back in action today, that I put the arbor in the freezer for a few hours, and then reinstall the arbor! It was such an easy fix, I wished I had thought of it. By substantially chilling the arbor down, the metal contracted in size. When the now slightly smaller unit is reinstalled, it’s able to go that much farther into the spindle. As it reached room temperature again, the metal expands, and the fit is ultra tight. It worked like a charm! I sped up the process to under an hour, by placing the arbor (protected) outside. My shop is just outside of Boston, where the temp. was around 5 degrees.
I got a kick out of this new trick, and thought you might too.
Dan Kornfeld, Owner/President – Odyssey Wood Design, Inc.
Replies
Dan,
Nice trick, thanks for sharing. When that happend to my new 17" radial drill press two years ago I just returned it for a new one. No problems since then..but, ya never know.
That is nice, and another example of thinking a little outside the box. I've known about shrink fits for years, but never thought to use it on demountable connection.
Another fix I've heard of is a very thin coat of rosin dissolved in alcohol. Clean shank and socket well, apply solution to shank, let dry, and install as before.
tried that trick a few years ago with my p.o.s. delta. worked fine until the day i had to drill a bunch, 500-600, of holes and after the first couple hundred everything had heated up and out it fell again. a little cylindrical bonding loctite (#609 maybe?) has kept it in place ever since.
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